After
The Flood
Monday
- Day One
The
flood occurred shortly before noon on Monday, 14th January 1895.
As soon as the situation became apparant, the pump at No 3 (Boyles
Hall) shaft was set to work at full rate. However, the pump at
No 1 shaft proved useless as it was surrounded by water and would
not work. Colliery managers set about trying to divert the water
into empty workings so as to give as many men as possible a chance
to escape. The last batch of survivors was brought to the surface
by John Boulton at around five o'clock in the afternoon, and no-one
was brought out subsequently. By Monday afternoon, Mr W N Atkinson,
HM Inspector of Mines, and Mr Joel Settle of the Madeley Coal & Iron
Company had arrived and had been down into the pit several times.
A search party comprising Messrs Atkinson, Mitcheson, Settle, Henshaw
and Maddock, came back up at seven o'clock were of the opinion
that it would be 24 hours before the water level dropped sufficiently
for the remaining trapped men to be brought out. In the meantime,
nothing could be done except to keep the pumps working.
By
nightfall, several hundred friends and family of the missing
men were travelling back and forth between No 1 and No 3 shaft
(some 600 yards) in the snow and slush in search of news. The
gas jets which normally gave light at the colliery at night had
been put out and the only illumination was from the moon and
miners' lamps. The pumping engine was raising 180 gallons of
water a minute but the water level had dropped just six inches
in two hours and remained four foot six inches deep at the bottom
of the shaft. George Burgess and Thomas Corbett, the smith and
carpenter, were using the cage in No 1 shaft to bring up debris.
It was hoped that once the obstruction near No 1 shaft was removed,
efforts might be made to reach those trapped in the East 7 foot
and 10 foot seams.
Tuesday
- Day Two
As dawn approached,
it became clear that there was no real chance of reaching the trapped
men from No 3 (Boyles Hall) shaft, so attention was turned to No 1 shaft.
Once the water level dropped there to around a foot, the Cameron engine
could be brought into operation. By six o'clock in the morning, the trapped
men had been below ground for almost 24 hours, with no food except what
they had taken down with them the previous day. Reports came that around
fifteen yards of debris had been cleared from the tunnel running from
the bottom of No 1 shaft towards the 10 foot dip - but there were another
15 yards to be cleared before the bottom of the 10 foot dip would be
reached. Men began to arrive at the colliery and changed into their working
clothes, waiting for their turn to descend and work on clearing the blockage
of debris.
Messrs Maddock and Mitcheson descended No 2 shaft to determine the water level
there, and found it was just below the roof, while the water continued to run
freely. They became concerned that as the debris was loosened, it would run
down into the sump and prevent any further pumping. However, they had no choice
but to continue with the removal, and accordingly the next group of miners
prepared to descend.
Throughout the early hours, each time the cage ascended, the waiting relatives
would crowd around to see if any survivors had been brought up, but each time
there was no news. By morning, the waiting crowd had dwindled to around 50.
By nine am, the pump had been reduced to seven strokes per miniute, for fear
of the sludge from the wall of debris blocking the sump. The water level in
the shaft had fallen to four foot 3 inches, and still the water was rushing
through the workings below ground. Twenty men were sent to fill up one of the
old gutter pits, from which water was pouring into Diglake. However, between
the hours of two and six am around a hundred square yards of clay and stone
had been thrown down the gutter shaft with no appreciable effect.
At around one thirty in the afternoon, an inspection was made, and it was decided
that work on clearing the obstruction at the foot of No 1 shaft should be suspended
as being too dangerous. The miners were working underground in water four foot
six inches deep, and progress was extremely slow. Moreover, the water level
showed no signs of falling.
Rain began to fall, and hopes of rescuing the still-unknown number of men trapped
below ground began to fade. However, the ventilation fan had been kept going
and the engine man stated that he could detect a leak somewhere, possibly caused
by the trapped men breaking into an air line in order to provide themselves
with ventilation.
It was by now generally acknowledged that the eleven or so missing men from
the West 8 foot seam must have perished; this seam was at a lower level than
the 10 and 7 foot seams and so would have flooded first.
In the afternoon, a decision was taken to descend No 3 shaft and try to lower
the roadway there, allowing the water to flow more quickly into the old workings
below. At twenty past five, thirteen men in the charge of John Sproston were
lowered into the shaft. They returned to the surface at nine o'clock that evening,
with the news that they had cut a channel through the head of the level and
that a large stream of water was now flowing into the old workings. At the
same time, measurements showed that the water level at No 1 shaft had falled
by a good eight inches, and it was decided that efforts to shift the blockage
near No 1 shaft could now be resumed. At nine minutes to ten o'clock a party
of six was lowered, including Mr Makepeace, Mr Frank Rigby and Mr John Watts.
Nine minutes later they returned - with the first body to be recovered from
the flooded pit. The dead man had been found amongst the debris which formed
the main blockage between the shaft and the 10 foot dip.
At ten-thirty pm, the cage descended again, returning an hour later with the
news that they had found a second body, trapped beneath a waggon which formed
part of the underground blockage. It was their opinion that removing the waggon
would cause a large amount of debris to be swept directly into the pump.
Wednesday
- Day Three
At
ten minutes past midnight, another team of men led by Elisha
Mayer was lowered into No 1 shaft, and they returned twenty minutes
later with the body which had been discovered late on Tuesday
night. The body was identified as Harry Rhodes, a breaker from
Boon Hill. Between two and three o'clock in the morning, the
men suceeded in reaching the pumping engine at the bottom of
No 1 shaft, and preparations were made for getting it started.
But by seven thirty that morning, the Cameron pump still lay
idle, it's suction pipe still blocked by quantities of dirt.
Yet still the air continued to circulate below ground, leading to the faint
hope that some of the men at least remained alive down there.
The first body to be recovered was identified as Charles Vernon of Wood Lane,
a man whose father had been killed in the Talk'o'th'Hill explosion of 1866.
Later on Wednesday, it was realised that the man was actually Henry Holland,
a friend of Charles Vernon's. In life he had often been confused with his friend.
Efforts continued to clear the blockage to the 10 foot dip, and relays of men
continued to work waist deep in the freezing water below ground, but as night
fell on Wednesday evening, still the Cameron pump would not work, and the clearing
of the blockage was painfully slow - but was progressing.
Late on Wednesday night, a rumour spread that sixty men had been brought up
out of the pit alive. Relatives rushing to the pit were bitterly disappointed.
Thursday
- Day Four
At
eight o'clock am the Cameron pump was finally started, and made
good progress in reducing the water level. However, efforts to
clear the blockage were stopped by a waggon which was so entrenched
in other debris that, despite hours of work, it could not be
moved. A distance of twenty yards from the shaft had been cleared,
but now work was at a standstill. After an inspection at quarter
past two in the afternoon, a plan was formed to try and cut a
passage around the waggon.
The inquest was opened at the Plough Inn, Audley. A half-holiday in the Potteries
had resulted in many spectators visiting the pit to see for themselves the
state of affairs. By quarter to seven in the evening, work was still at a stop.
By quarter past, the plan to cut a new crut had been abandoned, and it was
accepted by all that a vast quantity of water still remained in the old workings
and was making its way into Diglake pit, and that hopes of finding anyone alive
now were practically nil. At eleven o'clock that evening it was estimated that
20 tons of water per minute were still rushing through the pit. Mr Watts, the
manager, stated that it would be a matter of months before the debris was removed
and the bodies recovered.
Friday
- Day Five
By
Friday morning, most of the crowd waiting at the pit head had
disappeared. The pumps were raising 300 gallons of water per
minute, yet still the water level failed to drop. Work to clear
the debris continued into the afternoon.
Saturday
- Day Six
This
morning, a telegram was issued by the pit management to the effect
that work to clear the blockage underground was being called
off. It was felt that it was "cruelly wicked" to ask
the men to continue working in such conditions any longer, particularly
since the threat of gas had joined with the possibility of a
sudden roof fall or inrush of water claiming yet more lives.
Pumping would continue, but all work undergound would cease.
On Saturday evening, ten more pit horses were brought to the surface, as well
as a cat and two kittens.
The railway line some 500 yards from Audley Station, next to Diglake Colliery,
was sinking, as a consequence of the collapse of one of the old pits which
was pouring its water into Diglake.
Whether
or not the 40 or so men trapped underground in the East 7 and
10 Foot seams were still alive, no-one will ever know. In the
1860s during a flood at Boyles Hall Colliery (of which one shaft
now formed Shaft No 3 of Diglake Colliery) a man had survived
for three days underground - by consuming his supply of candles.
This man's name was Sproston - possibly John Sproston, Diglake
undermanager.